Category: Random Projects

Small to-do items that aren’t part of a larger project

Water Heater Distractions

The inspector from the bank will be coming around to check on progress. Among other things, I’m hoping to get reimbursed for a rather large bit of radiant heating expenses. In order for that to happen, there needs to be visible progress on the radiant. So that was my top priority…until the water heater went on the fritz.

Not having hot water is a rather immediate problem. The issue was that it was short cycling, so while it was getting hot eventually, in the meant time we’d run out of hot water. I bought the silly thing to prevent that exact problem, and since it was rather expensive, I really don’t want to kill the thing with short cycling.

In the extremely likely event you don’t recall, I have an AO Smith GDHE 50 “Vertex” direct vent condensing 50-gallon water heater. It’s a natural gas combustion heater with a blower, and intake and exhaust lines through the roof. The thing has been through a lot. I originally installed it in the basement, I had to replace the flame sensor after the basement tuckpointing clogged it with dust, I moved it up to the first floor when we redid the basement, moved it back to the basement and it was hooked up by the (previous) plumbers, and then Dean and I re-ran the intake and exhaust from the side of the house to the roof.

It’s worked fairly well through all that. Other than the flame sensor, the only issue was when it was venting out the side of the house the intake would frost up because it was right by the exhaust from the boiler. Since running it through the roof, it’s been trouble free until now. I’ve drained and flushed it a couple of times to keep it in good health, but otherwise left it alone.

From above (blower removed)

I took a look and read through the service manual, and ordered another flame sensor. It seemed the most likely, and I wanted the part on hand if I had to take the whole thing apart. Once it arrived, I started working on the thing, and a collection of tools began to grow next to me: Phillips and flat head screwdrivers, adjustable wrench, nut driver, allen wrench, power screwdriver, hex bit, three bit extensions, socket wrench, measuring tape, pipe cutter, other pipe cutter, pipe wrench, rag, plyers, butane torch, solder, flux, needle nose plyers, gorilla tape, and shop vac.

Un-removable burner assembly

Needless to say, this was a long, frustrating process. I won’t bore you with all the details, just the highlights. The plumbers ran the water supply pipe directly over the center of the water heater, which meant I physically couldn’t remove the burner assembly (I admit to pretending it’s a reactor core). I wound up re-plumbing that, with only two trips to Home Depot only to find that my “shortcut” of using Sharkbite fittings was leaking, after which I just soldered everything. At that point I thought it was fixed and went to bed well pleased.

Easier access

I woke the next morning and took a nice hot shower, then discovered a puddle on the floor of the mechanical room and errors on the water heater screen. An existing fitting, one that I didn’t solder but next to one I did, started leaking. Apparently it got too hot when I was working on the adjacent connection and the solder failed. That flooded not just the floor, but the whole burner. This led to the shop vac, where I literally sucked the water out of the thing.

Water where it should not be (down in the exhaust pipe at the bottom)

At this point it was behaving a better than it had when I started, and I had completely worked out the process to remove the blower and burner, but it still struggled to get through a full heating cycle without an odd gurgling in the exhaust drain line followed by a purge and restart. I checked all the things I could think of, made sure the condensate hose had a trap, cleaned the chud out of the cleanout, checked exhaust pipe slope, but eventually, I went to work on the radiant panels.

Overdue Updates

Wow, three months without updates, almost exactly all Winter. That’s an ignominious record for us. Despite that long dry spell of writing, we have been working on the house. Life has been extremely busy, as it tends to be. The list of excuses is long, from holidays, winter illnesses, work craziness, Wednesday swim lessons, literally all of Diablo III, and an aversion to working on the house when it’s cold and gets dark at four thirty. Quite honestly a large reason for the lack of updates is because I no longer have time at work, we only have one computer set up at home, and Sarah’s been working in the evenings. But! Tonight she’s on the phone with her mom, so let me try to get something written.

In Progress: Left window old, right window new

With the last post back in December we put in the first front window on the second floor. Mike helped with a lot of the exterior work that followed. We started with the two side windows of the front bay. We’re leaving the center window of the bay because it’s our way onto the porch roof. We stripped off the rest of the siding on the front of the house and removed what was left of the original front gable soffits (rake). We framed the new opening for the attic window and got the rest of the front of the house covered in house wrap.

Next we tackled the roof of the bay. That was a big project, since the old bay roof was flat and the new roof comes to a point. More than that, despite moving the new attic window up, it was still in the way of the bay roof, so we had to cut the height of the bay walls down by about six inches. Mike cut some insane angled birdsmouth rafters and I mostly stood around holding things. We have that covered in ice and water shield to keep the rain off.

Attic window framing, ice and water shield on bay

I came back and tried to get the attic window installed, since we had just covered the opening in house wrap and it was flapping like a drum in the wind. I got the jamb extensions on and the house wrap in correctly, but when I went to put the exterior rigid foam on I realized that without the rake, cutting the foam accurately was not going to happen, so I switched gears and started working on the rake. I framed a ladder from 2x4s and then had to haul the thing up a ladder and try to screw it to the house. I realized that I’d made it too big because math is hard, took it back down, made it smaller, hauled it back up, then needed Sarah’s help to hold it while I cut back a piece of wood that was sticking out of the side of the house. The process took so long I only got the one side up, so I have yet to finish the window. Attempts to do the other side in subsequent weeks have been thwarted by the same types of excuses I listed above.

Front of house progress

During this progress on the outside, I’ve also continued working on the attic floor joists, but I still plan to cover all of that in its own post, which hopefully I’ll actually get around to writing. It’s Spring now and I’m really trying to get back in the saddle.

Unexpected Plumbing, Yet Again

At some point I guess we should just expect unexpected plumbing to happen. However, I can say with certainty that we didn’t expect a loud thud followed by a cascading shower of water from the mechanical room ceiling one fine Saturday evening. We’d just gotten the kids into bed and Sarah was doing dishes when it happened. I came running from the living room (one of us has to sit watch so the kids stay in bed and go to sleep) and she was already pointing me out the back door and upstairs.

Cast iron pipe dropped

When we got upstairs we saw what had happened: one of the three cast iron soil and vent stacks in the wet wall had basically fallen straight down about two feet. The straps holding it in place were both snapped, the top of the stack was in the attic instead of sticking through the roof, and most critically, the PVC pipe it connected to at the bottom (where the washing machine drains) had cracked at the main stack and the waste water from the washing machine had poured out of the broken pipe end into the basement from above.

Broken fitting

The good news is that there wasn’t any serious damage. The 2″ cast iron pipe was already slated to be removed, nothing in the mechanical room that got wet was harmed, and the PVC section connecting the washer was temporary. We turned off the washer and went to bed, leaving the problem for the next day.

Vent stack dropped out of roof

Sunday morning I started by removing the cast iron pipe. This drain used to be used by the kitchen drains from the first and second floors. Apparently, it had been supported by the plaster and lath of the walls, and with only the straps (and the PVC pipe underneath) holding it up, it simply gave way. The bad news was that the PVC had cracked at a fitting, right before it went into the main stack, so I had two options: use a heat gun, some pliers and about an hour to pry the remains of the fitting out and try to re-use the Tee, or cut out the 4″ PVC stack section and put in a new one. That seemed easier, so I ran to the store and got some supplies, including a 10′ section of 4″ pipe.

Pipe removed

I managed some Three-Stooges-level incompetence when it came to removing the old PVC pipe section, spilling the remaining water inside at several opportunities before finally getting the rest into a bucket and the pipe out of the wall…before knocking over the bucket on the floor. I did my best to clean up the new mess on the subfloor and Sarah put down even more towels in the mechanical room below. I put together a new branch for the washing machine and glued it together with minimal fuss.

Roof penetration

The final step was to patch the hole in the roof. When I got up on a ladder in the second floor and took a look, I found the expected congealed tar, but also some bent aluminum flashing. Because I didn’t want to get onto the roof and do a more extensive repair, I simply put some flashing tape over the aluminum cylinder from within.The roof (and walls) already leak, so it doesn’t need to be perfect at this point. We’ll be putting on a new roof in the not-too-distant future and it’s Good Enough™ for now.

Unexpected Plumbing, Again

I thought we were done with this. When we moved into the basement, we were finally using the new plumbing exclusively. The old galvanized pipe was completely disconnected and I assumed that meant our random plumbing issues were behind us. Unfortunately, that turned out not to be the case, and the cause was one we’ve become quite familiar with: freezing. All our pipes are in the basement, which is heated, so here again, I thought our frozen pipe problems were in the past as well. Of course, there’s an exception: the washer and dryer are on the unheated first floor. Our original plan was to fit them into the basement while we are living down here, but we didn’t have much room and we opted instead for our dishwasher.

The plumbing lines that goes up the first floor is new copper, and it has a quarter-turn valve about 18 inches above the floor level in the wet wall. We’ve been shutting off that valve and draining the water past it when it gets really cold so we don’t break our washing machine (again). We noticed water dripping in the mechanical room and investigation revealed that the valve itself had failed, with water dripping from a seam in the valve body. Presumably this is due to freezing.

I went to Home Depot and of course they were out of stock, so I went to Menards and picked up the replacement valve and some sundry other supplies. Then I discovered I was out of flux, so I went back to Home Depot for that, so in other words it was a typical project. I managed to solder in the new valve with a length of pipe and a male adapter so I could connect our temporary PEX washer pipes. I also capped the hot water line, which I’d been meaning to do for a while. Finally, I wrapped all the pipes in the heating cable and covered it in pipe insulation that we had lying around from previous frozen plumbing escapades.

Water is no longer dripping in the mechanical room and hopefully we won’t have any further plumbing mishaps. I’m starting to work through how all the new drain and vent will be run, since I need to remove the remaining old stuff, and we obviously need a functional vent to the roof. I also pulled out the rest of the old supply plumbing from the second floor, so we officially have no more galvanized pipe in the house!

Unexpected Water Management

In my post about the sump pump, I discussed our concerns about water in the basement. Those concerns have proved well founded, because after some heavy Spring rains, it happened. Our interior weeping system directs water under the concrete slab to the sump pit and the sump pump pumps it away, and this system is working great. However, water doesn’t always come from below. Because of the thick, clay soil, water following the path of least resistance can come right through the brick basement walls. That water is coming in above the footer curb in the basement and then drains onto the top of the basement floor, bypassing the weeping system completely.

There are ways we could have avoided this. The preferred method is to excavate around the outside of the house and install a water barrier on the outside of the basement walls, but our house is less than four feet from the neighboring houses to either side, risking structural collapse of both our basement and theirs. Another method is installing a dimpled plastic membrane on the inside of the basement walls that provides a path for water to drain down below the slab and into the interior weeping system. We didn’t do that for a couple reasons. First is the potential for damaging the bricks, both from persistent water and from freezing. Second is that the membrane would have to wrap over the footer curb, and we’d have to frame walls in front of it, further reducing our floor space (by about 50 square feet). While we do plan to insulate inside the brick walls, we’re going to do so without a vapor barrier, so that the bricks can dry if they get wet. The interior-facing side of the footer curb will remain exposed, or at most covered by trim.

Old downspout accordion

Old downspout accordion

While we’re exploring ways to divert water that comes through the walls, the bigger focus is on keeping water away from the basement walls in the first place. Recently it poured, and I discovered that the downspout I’d put in after we removed the back porch was clogged, causing a fountain at the back corner of the house right where we were getting most of the water. Once I fixed that, the downspout was splashing about fifteen feet into the back yard… and then running across the patio to the other corner of the house. Worse still, our neighbors’ downspout was clogged and all the water from half their house was cascading into the gangway. The downspout we had on that side was running across the gangway and wasn’t sloped away from the house, so water was draining to the same corner. I got the water from both our gutters to divert to the stone-filled catch basin, but something more permanent was needed.

I ran to Home Depot and got some supplies, then got up on a ladder and reconfigured our downspouts. The gutter on the gangway side now drains across the back of the house between the first and second story, where it joins with the other downspout. It then drains about twenty feet from the house, but I plan to extend that to thirty. I also unclogged the neighbors gutter and ended the waterfall in the gangway. Since making this change we haven’t seen additional water, but I’m not yet convinced we’ve solved the problem. I have some other steps I can take if we see any more water.