Page 43 of 59

Unexpected Plumbing

Plumbing wall

Plumbing wall

After the demo party my mind was set on clearing out the rest of the lath. The dumpster was completely full, but we ordered a new one that was being delivered on Thursday. Wednesday evening I went down to start pulling up the subfloor in the kitchen and the floor in the foyer and I noticed a drip coming from the plumbing wall. It wasn’t too serious, so I propped a bucket under the pipe, supported by a board, and went about my work.

Wednesday night as we were falling asleep, we heard a crash from the first floor. The bucket had filled enough that it slipped and fell to the floor. Thursday the new dumpster arrived, but rather than getting to work filling it I  had to deal with the leak. It had gotten significantly worse and was splattering water all over. The leak was coming from somewhere up in the wall, in the second floor. I climbed up a ladder and shined a flashlight on the culprit: a pinhole leak.

Leaky pipe

Leaky pipe

The rusty spot was spraying water with aploumb, serious enough that it needed to be dealt with immediately. I turned off the water and determined that the pipe goes to no where. In the picture above you can see the yellowish pipe goes up and elbows into a tee. That is the supply pipe, coming from the basement. The top of the tee leads to all of the second floor fixtures. The bottom pipe, the one with the leak, goes down about eight feet and is capped. I believe it was the original supply pipe but it’s hard to say. The plumbing is old galvanized steel and has clearly seen some modifications over the years. For example, in the first floor wall there was a capped line going to about head height in the bathroom (and not to a shower head): it used to service a toilet with an elevated tank.

Because the pipe wasn’t connected to anything I decided it would be easiest to simply remove it and cap it, rather than try to patch the leak. In hindsight, I absolutely should have patched the leak. The same corrosion that had weakened the pipe to the point that water could simply push through the metal had made the threaded joint so impossibly strong that it would not come loose despite hours of prying on it with a pipe wrench. Part of the problem is that the tee that it connected to is up in the wall and I couldn’t get a second wrench on it.

I worked on it all evening, and once Derek was in bed Sarah came down and the two of us worked on it until about midnight when we finally gave up. With the water still shut off and the pipe partially disassembled, I took off work on Friday. Friday morning I was back at it. Since the water was already shut off I removed all of the first floor supply plumbing, something I’d been meaning to do for a while anyway. I took the bus over to Home Depot, since Sarah had the car, and picked up some supplies.

After liberally applying PB Blaster, heating the fitting with a propane torch, and using an 18″ pipe wrench with a four foot pipe as a breaker bar, the pipe still would not give. Finally, cursing pipe wrenches that slip and galvanized pipe that sucks beyond reason as a water pipe, I gave one more frustrated push and it gave way, or at least so I thought. I unscrewed the pipe and pulled it down from the ceiling only to discover that the pipe had not, in fact, come out of the tee, the tee itself had sheered off the elbow and come out with the pipe.

The accursed pipe, pinhole leak and still-attached sheered off elbow visible

The accursed pipe, pinhole leak and still-attached sheered off elbow visible

Now instead of simply capping the pipe I was going to have to put two ends of threaded pipe together. That meant I needed a union, which meant I needed to go back to the hardware store. Just then it started raining outside. Looking at the dangling supply pipe I realized that it wasn’t the cold water pipe I was dealing with but the hot, which meant I could turn off the valve at the hot water heater and turn the water back on, allowing the use of the toilet and sinks. In fact, I could have done that Thursday night and not been without water for twelve hours.

I trudged over to the hardware store, bought the union along with a 3/4″ to 1/2″ reducer and came back. In one more oddity of the plumbing of the house, the pipe from the hot water heater is 1/2″, but the tee it connected to was 3/4″. That meant my reducer was actually going to be an expander, something you really shouldn’t do with plumbing.

Replacement pipe

Assembled replacement pipe

I removed the upper segment of the hot water pipe and took off the broken elbow. Then I put together a new section using the expander and a section of salvaged pipe, along with a coupling. I put this on the end of the hot water pipe segment and reconnected it to the fitting up in the wall with a lot of teflon tape. Finally I put the union onto either end of the pipe and connected it together. It was finished, or so I thought.

I turned the hot water back on and immediately a drip started. After shutting it off I inspected and found that the drip was not from any of the fittings I had put together; it was from the tee I had connected to up in the wall. There was a leak on the side where a pipe connected it, probably torqued by the earlier wrenching much as the tee that had sheered off had been. Removing this section was not an option. There was no way to get to it without completely opening up the wall behind the kitchen sink on the second floor. Because the leak was small I found some plumbers epoxy and wrapped the whole fitting in it and waited twenty minutes for it to cure. When I turned on the water again there were no leaks.

Repaired and patched pipe

Repaired and patched pipe

You can see the fitting globbed with putty. I actually added some more after taking this picture. I want to point out that taking these photographs up in the wall using the flash and getting the focus right while I was on top of a ladder is incredibly challenging. I hope you appreciate the effort. In hindsight I should have patched the pinhole leak with the putty and been done with it, but I had forgotten that I had it (I bought it for the condo) and after discovering that the leaky pipe didn’t go anywhere I really thought it would be simplest to just remove it (obviously not).

After all of this, the inevitable crud that was broken loose inside the pipes spit brown chunks from the fixtures for a couple of minutes. Even after cleaning out the aerator on the kitchen sink faucet its pressure was abysmal, while the other fixtures worked fine. Because it was slow on cold and hot water I knew it was the mixing valve. Saturday I took the faucet apart and cleaned out the cartridge and got it back up to its normal mediocre performance. I look forward to replacing all of this garbage with copper. Unfortunately for the time being we’re stuck with it.

Stairs Demolition

Saturday we had our second “Demo Party”, where we invite friends and family to come demolish our house in exchange for food and drink, and it was a big success. We took down all of the plaster and lath in the foyer, including the stairwell, as well as the office on the second floor. Then we took out the remaining partition wall on the first floor and removed the stairs themselves.

Aaron and David get walled up

Aaron and David get walled up

Sarah and I had gotten the office empty Friday night. My sister Jessica came up and watched Derek while we continued the furniture rearranging and packing away of our stuff that we’d started Wednesday. Saturday morning two of her nephews, Aaron and David, armed with sledgehammers and masks volunteered to be the “trapped princesses” and went into the office while I built a wall where the door was. Once they were completely walled up, rather than wait to be rescued they simply hammered their way through the wall adjacent to the stairwell.

Breaking free

Breaking free

Sarah K, Dani, Matt B, and Eriq hauled the massive pile of lath was out to the dumpster along with the scrap wood pile. Unfortunately even before we got all of the lath into the dumpster we realized we had a problem: the dumpster wasn’t big enough. I had gotten a smaller dumpster than last time, foolishly believing that since we were demoing less we wouldn’t need as much room. I forgot to consider that the lath and scrap wood pile were leftovers from the last demo. Now I have to get another dumpster, which costs quite a bit more than if I had just gotten the big one in the first place. Oh well, I’ll know for next time.

Demo in progress

Demo in progress

The house didn’t originally have electricity, just gas lighting, and I spent a few minutes on Saturday taking out the piping that was still in the walls. It was retrofitted with BX armored cable with cloth-wrapped wiring, which  was run through the load bearing wall by threading it under door thresholds in the second floor and then down between studs in the wall. I disconnected all of this wiring a while back, but a lot of it was stuck, hanging from the ceiling.

Removing BX wiring
Removing BX wiring

Eriq, Will, and I took on the task of removing it. This involved literally climbing up the wall and alternately pushing and pulling the metal-armored cable through one segment at a time. I can’t imagine how this was put in while the walls were still plastered considering how hard it was to remove. We did manage to get all of it out and the only thing left to be removed from the bearing wall is a gas pipe that goes up to the attic for distributing the gas lighting.

Dean clearing lath

Dean clearing lath

Dean was able to get all of the ceiling in the office and stairwell down from above by getting into the attic. This also meant he didn’t get rained on with plaster dust and rat feces. I shoveled the plaster from the floor of the office down the stairs while Siobhan, Sarah K, Dani, and Matt B filled buckets and carried it to the dumpster. I filled and carried out buckets while Dean took the exciting job of getting on the ladder over the stairwell –sixteen feet up– to remove all of the plaster and lath from the walls.

Dani and Matt B on plaster removal

Dani and Matt B on plaster removal

The old lath pile was replaced by a new pile as the foyer demo was wrapped up and we got to work taking out the stairs. This took alternately a reciprocating saw and a sledgehammer to pry each tread loose, working our way down. When it was all said and done, the difference was incredible.

Sarah and her mom baked up lasagnas so we could wash up, eat, drink, and finally relax. This week the new dumpster will be swapped in and I can get the rest of the piles cleared out of the house, along with the plywood subfloor in the kitchen and a couple layers of flooring in the foyer.

A big thanks go out to everyone who gave up their Saturday to help us! Aaron, David, Eriq, Matt B, Sarah K, Dani, Dean, Siobhan, Will, Mike, and Lee, we couldn’t have done it without you!

Goodbye Original Floors

The first floor originally had wood floors throughout, as was typical of the time it was built. These were floated on furring strips running across the subfloor. The bedrooms had a 4 1/2″ wide plank and the rest was 3 1/2″ wide, each different types of wood, 3/4″ thick. On top of this flooring someone had installed (nailed) a second layer of wood flooring, much thinner or possibly just refinished many times. On top of that was a variety of multiple layers of linoleum and vinyl adhesive tiles and in a few places carpeting.

Back in August we removed all of the flooring down to the original wood floors before our demo party and the debris was put into the dumpster. The dumpster was completely full so we wound up stacking the original floor in a big pile in the kitchen, with a big pile of the furring boards next to it. It sat there gathering dust for the next six months.

Original floor

Original floor plus dust

We took up the original floors for a number of reasons. First, it was in terrible shape. While an indefinite number of layers of tile can be removed and sanded down, the wood floor nailed down on top of the original floor had done a lot of damage. Second, we’re putting in radiant floor heating, and a floated hardwood floor does not work well with that. That leads to the third reason: since we’re opening up the floor plan and the flooring is different woods, sizes, and styles, refinishing it as a single floor wouldn’t look very good. Finally, there wasn’t near enough of it. In addition to the various walls we’re removing that would call for new flooring to fill in gaps, the entire kitchen floor had been removed at some point and replaced with a plywood subfloor. 

So, getting back to the pile, Sarah had looked into selling the floors or getting someone to take it away but they wanted us to de-nail it first. While it may have ended up being a profitable venture, it represented a lot of time that neither of us had to spend. Finally, I put an ad on Craigslist.

I specified in the ad that there was a large pile of perhaps 500 square feet in mostly twelve foot lengths of various usable and unusable quality, that it would require a large truck or multiple trips, and that it was take all of it or none of it, for free, first come, first to get it. I got a bunch of responses right away, and I went with the first one. This proved to be a poor choice.

Two guys showed up a few hours later in a Hyundai SUV. It had no hope of carrying all of the flooring, and he seemed rather surprised when the pile was larger in person, despite the above picture being attached to the ad. They started loading it on to the roof of their car and I helped by bringing it out to the easement. Then they started bringing it out to the easement instead of putting it on the car. After loading about half what the car could probably carry, they said their storage unit closed at eleven and they wouldn’t be able to get the rest until tomorrow. They helped me move the remaining pile from the easement to the yard, and Sarah covered it with a tarp.

The next day I got an email from the guy saying they didn’t have any more room in their storage unit and couldn’t take the rest. Rather than dwell on my irritation, I quickly emailed the other respondents and let them know some of it was still available. Only one replied, but said that he’d be happy to come out and get it. However, when he arrived he took a look at the pile and said there was no longer enough salvageable floor to complete his project and left without taking any.

No, that's not all flooring

No, that’s not all flooring

This past Thursday, Sarah hauled the ignominious pile from our front yard into the street to reserve a spot for the dumpster, since the city hadn’t gotten around to putting up no parking signs. The dumpster arrived on Friday and the flooring went into it. It seems a waste, but I really can’t stress enough what bad shape it was in. As for everything else that went into the dumpster, I’ll be posting about the demo party we had on Saturday soon.

Next Steps

Back in August we had  a demo party and gutted most of the first floor, but we left the front foyer and staircase because we knew it would be a while before we were ready to start framing, plus we didn’t have our building permit yet so we wanted to leave the front entrance intact. Now, with the steel beam in the basement and the permit taped up in the window, we’re ready to get to work.

That means it’s time to gut the foyer and stairs, so we’re having another demo party this weekend to do just that. With a dumpster and people coming to help, we decided to demo the office on the second floor while we’re at it. The reason for this is when we rebuild the stairs that go from the first to the second floor, we’ll be putting them about five feet further back in order to make the front bedroom bigger. Moving the stairs back means the top of the stairs will be in what is now our office, or the middle bedroom on the second floor.

Last night we started cleaning up our mess in the office and finding places to put the furniture. Some things are going into storage in the basement, but we still need to move our only phone jack so we still have Internet and figure out where to put one of the desks.

Once the demo is done we’ll be able to close up the remaining window on the North wall and replace the load-bearing wall that runs from front to back with an LVL beam and columns. LVL is laminated veneer lumber, an engineered beam that is stronger and stiffer than wood. That will allow us to have the open plan we want while still properly supporting the second floor.

The open question is whether or not we should build temporary stairs or make do with the stairs on the back porch. It’s going to take some time to get the beam in place, re-frame the joists both in the floor and the ceiling, install new subfloor, and build a proper set of stairs. We might be able to build a temporary set of stairs in the mean time just by cutting some stringers and reusing the existing treads. The only trick will be the winders that we have now. I may just build a landing and make the straight run a bit longer, but I’m not sure yet if that will fit.

Beam Project: Steel

Friday, Mike went to Suburban Welding and Steel and picked up the three pre-cut beam sections totaling about 45′ and one 20′-long piece of square tube steel to cut into columns. He has a big pickup with a rack on the back, so they were able to lower the steel onto the back with a crane. Total cost came to $1,083. Saturday morning I picked up some donuts and made some coffee and people started showing up. After a little bit of work getting the front basement window opened all the way and and the gate to swing wider, Mike got his truck angled up to the curb and we unloaded the first 384 lb, 16′ beam section. Predictable this was actually the last section we needed to put in, but the way they were loaded on the truck didn’t give us much choice. We fed it through the window and set it on a couple of ladders in the basement.

Old beam removed

Old beam removed

Next we started taking out sections of the old beam. We got a bit of a surprise when a couple of 2x4s in the ceiling for drywall nailing edges were pulled down with the beam. This was especially alarming because they nearly pulled down the gas pipe that ran under them! Fortunately the pipe didn’t rupture and we were able to remove the 2x4s and re-anchor the pipe to the ceiling. The rest of the beam came down without incident and the temporary wall showed no signs of any problem carrying the load.

Cutting the beam

Cutting the beam

There was a slight miscommunication about one of the beam measurements so Mike cut a couple of feet off, but better too long than too short. He has a fancy gas-powered saw for just such a purpose. Having someone that not only knows how to do the job, but has the tools necessary to do it was critical to us being able to tackle this ourselves. With the beams cut down we used the jack posts to hold them in place. Then Mike ran a string line from one end to the other to that we could line them up properly and get everything level with the hydraulic jacks.

Positioning the beam

Positioning the beam

We used clamps to hold the two beam sections together because it was slightly torqued. Then Mike used his arc welder to weld the beam sections together. Normally the separate sections are just bolted together with a steel plate, but this will be stronger and hold everything together better. Next up was the columns. Dean took a turn with the big saw and cut the columns.

Cutting the column

Cutting the column

The columns were a tiny bit too long, so I used the angle grinder to trim them down about an eighth inch. When we went to fit them again they were still too long, but it turned out one of my hydraulic jacks wasn’t quite holding pressure and the beam had just dropped slightly. We pumped it back into place and fitted the column in. Mike welded the columns into place, directly to the beam at the top and to a steel plate notched for the bolts at the bottom.

Dean and I tried our hand at arc welding on the base of one of the columns, which was a really interesting experience. There’s a strange balance between keeping the end of the stick from touching the weld so that a spark gap is created while still continuously pushing the stick in so that it is consumed. We used the rotary hammer to drill holes into the footing for the bolts and pounded them in, tightening them up so they were good and snug. It was done.

Finished beam

Finished beam

Today I took  down the temporary wall and got my first look at the basement completely opened up. I’ll still need to paint the beam so it doesn’t rust and Mike thinks I should put a column at either end since the ends of the beam are pocketed into the brick, which isn’t in terrific shape. At some point I’ll bring in a tuck pointer to clean up the brick foundation inside and out and we’ll see if that does it. Otherwise we’ll have a bit more steel work in our future. You can also see from the picture that I have a lot of cleaning to do!